I have a Bosch RA1181 router table. I'm using the fixed base of my
MRC23EVSK router in the table.
The Bosch fixed base (MRF01) has a design flaw, I think. I wonder
about the best way to deal with it.
With the fixed base mounted upside down under the table's top, the
router motor placed in the mount, and the clamping lever loosened, all
of the weight of the motor is supported by the retaining snap ring
(e-clip) attached to the adjustment shaft. This is a very weak
The retaining clip (e-clip) is held in the adjustment shaft by a
shallow groove in the shaft. When the shaft is turned to adjust bit
height, the ring can--and does--slip out of the groove so support of
the motor is lost.
Has anyone else run into this problem? Did you find a way to avoid
Not a design flaw, you are simply using a router that was intended to be
used in the traditional manner, not upside down. so you have to be
careful to not damage the router.
What you should be using is one of these.
(Amazon.com product link shortened)
or any of these
Or use the plunge base for that router.
Well, I'm using a Bosch router motor with a Bosch fixed base in a
Bosch router table. Certainly, the Bosch engineers must have realized,
when they designed and marketed their router table, that their motor
and base would be used in the table. It's shown used that way on p.23
of this manual:
It's clear to me that the base was not designed to be used upside down
as it is in the router table. For that reason, I have to label the
weakness that I described as a design flaw.
I will give these two links a careful review but I'd rather not have
to buy additional equipment.
That would be a problem. I use the plunge base fairly often and
wouldn't want to have to remove and reinstall it in the table. The
fixed base is permanently installed in the table since I haven't
needed it for any other reason. Also, since the base is spring loaded,
it would be awkward to use upside down under the table.
I don't have that router, I have 2 of the 1617evs.
But I wonder if you can add a drop of C/A to the circlip or eclip .
First take it apart and wax the area where the circlip or eclip rubs
against so it won't glue to that area. you can also use oil, but if you
drop the clip into it, it defeats the purpose. use a heavy coating of
wax as c/a will still burn though, or better yet, use waxpaper.
put the clip on, and drop the c/a on the clip and rod.. really just a drop.
If you even need to take it apart, a torch or soldering iron will help
you losen it.
That should help hold it.
I looked at that router, seemed way heavier than my 1617evs.
Other than that issue , how do you like it.
Rather than the c/a, I was thinking that a small (small!) hose clamp
might be used around the adjustment shaft to backup the clip. It's
only a thought at this point since I haven't studied the idea yet.
I think my router and the 1617 are in the same class with the 1617
being an older model. With the exception of the problem we're
discussing, I think the 23EVS router is excellent. The feature I like
most is the on-handle power switch.
if you plan to keep it then you should contact bosch if it is possible
some places have so many layers that you never get any traction
meanwhile i would not use it as it is because it sounds like the bad
kind of surprise waiting to happen
it is possible that the designer of the table was not thoughtful
enough and also was not in contact with the designer of the router
I do plan to keep it. The only "surprise" occurs when adjusting bit
height from above the top of the table: the e-clip can slip out of the
groove on the adjustment shaft and prevent the motor from being
raised. Everything is safe once the base clamp lever is engaged.
I've come up with a fix. I wrapped some plastic material around the
1/4" adjustment shaft (to increase the diameter) and against the clip,
then tightened a small hose clamp (minimum 5/16" diameter) around the
plastic. This seems to work. The arrangement is secure on the shaft
and the clamp doesn't interfere with the motor or anything else.
That's good, but there's a better idea.
A better fix is to place a T-nut big enough to just slip over the 1/4"
adjustment shaft (5/16"?) and use the hose clamp and plastic to hold
it in place. This way the flange of the T-nut rides against the base
flange that the clip rides against. I haven't tried it yet but I think
this is a better way.
I'm adding this post for anyone interested or anyone who has run into
the same problem. I've implemented a fix that has worked for me.
After removing the e-ring, I drilled out the threads of a 1/4" T-nut
using a 1/4" drill, then slipped the T-nut over the threaded shaft.
With the shaft correctly mounted in the base and the flange of the
T-nut against the flange that the e-ring rested against, scratch a
mark around the shaft where the other end of the T-nut sleeve meets
Now remove the shaft and the T-nut from the base.
Using my drill with a diamond cutting wheel (a few bucks for the wheel
from Harbor Freight), cut a groove around the shaft. Let the groove
extend from about 1/16" above the scratch mark to about 1/16" below
it. Cut the depth of the groove so that the final diameter of the
groove is about half the diameter of the shaft.
Using some abrasive, such as sandpaper, abrade the surface of the
shaft to roughen it.
Clean the shaft and the T-nut with acetone to remove all oils and
Assemble the shaft and T-nut back onto the base. When the shaft and
T-nut are seated properly, the sleeve of the T-nut should extend about
half-way across the width of the new groove. The other half of the
groove should be exposed.
Mix a two-part, 5-minute epoxy. Glop the epoxy onto the end of the
T-nut sleeve and into the groove on the shaft, being sure to get epoxy
completely into the groove, up under the end of the T-nut sleeve. Be
generous with the epoxy. Spread it thickly, including over the end of
the T-nut sleeve and on the shaft beyond the groove.
Patiently watch the assembly after the epoxy has been applied. Prevent
the epoxy from forming a drip on one side or wetting down the inside
of the T-nut sleeve. You don't want to epoxy the T-nut to the router
base, only the threaded shaft. If you've used 5-minute epoxy, it
should stiffen fairly quickly. Once that happens, allow at least 24
hours for the epoxy to cure.
The threaded shaft should now be held securely in the fixed base and
the router lift feature should work reliably.
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